(Question details) Specific performance:Tube explosion and bulge of thermal fluid heater.Answer: Cause of failure:(1) Over temperature.(2) Over heating.(3) Hot oil metamorphism. Troubleshooting:(1) Emergency shutdown.(2) Oil discharge and fire extinguish.We use automatic control for operating, burning, high level tank level, outlet temperature and flowrate are all automatically regulated and protected to avoid overtemperature or overheating.
Question details (Performance):There is no feeding machine between hopper and # 0A/B belt, which causes unstable feeding and feeding amount cannot be controlled, during running, big amount material presses on belts which affect normal operation of the belt.Answer: The cause of the problem: Because the toughness of the biomass fuel is bigger, the proportion is small, material level should not be too high, otherwise it will occur block, so conveying system is normally running 24 hours, moving parts are easy to wear and cause high failure rate; also the length of the cut grass is difficult to guarantee its length between 8 ~ 15cm, and it is easy to get stuck in the feed machine before the furnace and it is difficult to clean, which has a great impact on the load of the boiler. Troubleshooting: 1. To reduce wearing and expand the service life of equipment, general motor adopts variable frequency motor, slow down the running speed, to control the rate of fuel feeding, make material's stacki
Question details (Performance):Dust collecting cloth bag damages a lot. Answer: The cause of the problem: As the biomass-fired boiler fuel moisture is high, and bag material is general PPS, which will reduce the base fabric of the bag in the case of high temperature, high humidity, hydrolysis, oxidation, and cause damage; In addition, the fuel moisture is high and it cannot be completely burned in the furnace, so it burns in the dust collector, which is also an important reason for the damage of the cloth bag.Troubleshooting:(1) Design by full consideration of high fuel moisture, choosing the appropriate induced draft fan, if the existing design is not enough then consider change the induced draft fan.(2) If induced air volume is sufficient, a proper distribution of the first and second wind should be considered. Generally, the fuel with high moisture and light quality such as wood chips, straw and wheat straw hood, the secondary air volume should be increased. For bark, miscellaneous
Question details (Specific performance):Biomass environmental protection and energy saving fuel made of straw and livestock etc., their combustion is not full. Answer: The cause of the problem:1. Air quantity is insufficient or too big.2. Outer flame position is not proper.Troubleshooting:1.Sufficient temperature: sufficient combustion of biomass boiler needs high temperature, combustion rate is proportional to the temperature, to raise the temperature as much as possible but guarantee there is no slagging.2. Proper air volume. If the air volume is too large, it will reduce the temperature of the furnace and increase the incomplete combustion of fuel. If the air volume is insufficient, the combustion efficiency will be reduced, and the waste of fuel will also increase the emission of smoke.3. Sufficient mixing of fuel and air. During the burning stage of biomass boilers, the sufficient mixing of air and fuel should be ensured and the disturbance should be strengthened during the burnin
(Question Details) Specific Performance:The pipe of superheater bursts in circulating fluidized bed boiler operation.The bed pressure indicator fluctuates little. Answer: causes of failure:(1) Design Factors.(2) Manufacturing process, installation and maintenance quality.(3) The temperature control device is unreasonable or does not work properly.(4) Effect of operating conditions on overheating and explosion of superheater. Troubleshooting:(1) Report the fact to operator on duty and require operating the boiler in low load.(2) When the overheat damage is serious,please report it to operator on duty and require stoping the boiler immediately to prevent blowout of the near pipes.(3) Adjust the steam temperature as much as possible within the normal range.(4) If the superheater tube is not damaged badly, it has little effect on the temperature level of the steam, and it can be allowed to run in a low load range for a short period of time.
(Question Details) Specific Performance:(1) The bed temperature has risen sharply.(2) The oxygen level drops even to zero.(3) The current of the primary blower is reduced, and the wind pressure in the wind chamber is high and fluctuates.(4) The furnace negative pressure increases and the induced draft fan current decreases.(5) Difficulties in slagging.(6) If coking in low temperature, the bed temperature, bed pressure distribution is uneven, the deviation is too large, the bed pressure, the plenum pressure, the bed temperature is not normal, and the local bed temperature measurement point is not normally raised or lowered.(7) The bed pressure indicator value fluctuates little. Answer: causes of failure :(1) Improper operation, resulting in overheated bed temperature and coking.(2) The primary air volume during operation is kept too small, which is lower than the minimum fluidized air volume, so that the material can’t be well fluidized but piled up, the temperature field of the entire
(Details on the problem) Specific Performance:Slagging pipe blocks during operation of circulating fluidized bed boiler. Answer:cause of failure:(1) The internal shape is caused by the limited expansion of the wear-resistant material inside the slag discharge pipe. The internal components of the slag cooler are deformed, affecting the fluidization of the slag cooler; the slag cooler is deactivated for a long time or a single slag cooler is selected for slagging, and the bed material in the deactivated slag cooler is bonded under the influence of steam, which being low temperature coke.(2) The operating personnel did not grasp the ratio of the fluidized air volume of the slag cooler. Inappropriate air volume ratio resulted in poor ash slag fluidization in the slag cooler. Troubleshooting:(1) Operation personnel should strengthen understanding of boiler operating conditions, adjust boiler parameters in a timely manner, set up the concept of boiler material dynamic balance, control boiler
(Question Details) Specific Performance:(1) There are blasting sounds in the furnace, and the furnace chamber is under positive pressure. There is smoke emitted from the combustion chamber in a leakage. In severe cases, the explosion-proof door of the boiler body opens.(2) Drum water level drops rapidly and the feedwater flow rate is not abnormally larger than steam flow. MFT acts when the water level is below -280mm.(3) Drum pressure, steam flow rate, exhaust temperature decrease, smoke temperature difference increases on both sides.(4) The negative pressure at the inlet of the flue and suction fan becomes smaller and the temperature difference between the two sides increased. (5) Smoke temperature decreases at the inlet and outlet of the cyclone separator, and the temperature of the material returned is low.(6) Bed pressure increases, bed materials clean, fluidization poof, bed temperature distributes unevenly and bottom slag discharge difficultly. Answer:cause of failure:(1) Fly ash